油膛口 的英文怎麼說
中文拼音 [yóutángkǒu]
油膛口
英文
aperture of oil chamber-
And the traveller leopold was couth to him sithen it had happed that they had had ado each with other in the house of misericord where this learning knight lay by cause the traveller leopold came there to be healed for he was sore wounded in his breast by a spear wherewith a horrible and dreadful dragon was smitten him for which he did do make a salve of volatile salt and chrism as much as he might suffice
旅人利奧波德與彼相識。蓋該學生騎士因故服務于仁慈聖母醫院之際,旅人利奧波德曾被一可怕醜陋之用標槍刺穿胸膛,負重傷, 13前往就醫。騎士曾於傷口上塗以大量揮發性油及聖油,予以妥善處置。This article aims at the boiler ' s problems in operation : 1 ) under nominal load, the smoke temperature at the outlet of hearth reaches 1200, far more exceeds 1050 the original designed temperature. this will always result in slag inside boiler and the temperature of overheater ' s pipe superheat, so that boiler cannot take nominal load and all these influence boiler ' s nomal operation heavily, 2 ) this article also studied the reason why the assistant oil becoming necessary when coal changes. during the nomal operation, many factors ( makeup of combustor and its disposal, smirch and encrust of water wall, excessive air coefficient, temperature of primary air, coal type and density of coal dust ) can deviate the designed working conditions, then affect the boiler ' s nomal operation
本文針對該鍋爐在實際運行中存在的問題:在額定負荷下,爐膛出口超溫、低溫段過熱器前煙溫高達936 ,遠遠超過815的設計值;噴燃器四周水冷壁結焦嚴重,過熱器管壁溫度超標,無法帶上額定負荷;甚至有時因燃煤質量的變化,必須投油助燃的嚴重情況進行了分析研究。在實際生產過程中,燃燒器的結構、布置,水冷壁的粘污、結垢,過剩空氣系數、一次風溫、煤種及其濃度變化等許多因素都會偏離鍋爐的設計工況,從而影響爐內的傳熱和燃燒,造成爐膛出口超溫、水冷壁結渣等問題。3. on boiler retrofit, the calculation of fuel burning, the heat calculation of boiler inside structure and convection section, and the design of structure parameter of feed water heat exchanger are made. the flue gas channels " resistance calculation and the boiler strength verifying are also carried out. replacement of water cooling wall improves heat exchanging and decreases loss of heat radiant
對鍋爐本體進行了燃料燃燒計算、爐膛結構熱力計算、對流受熱面結構熱力計算、鍋爐給水加熱器結構參數設計、煙道阻力計算及鍋爐元件強度校核等;改進了水冷壁布置使換熱效果更好,減少輻射換熱損失;改進對流段結構,更充分的利用爐膛出口煙氣余熱,提高熱效率;並且進行了煙氣阻力計算、熱效率計算和能量平衡測試,對改進后的稠油燃料和改進前進行了對比,燃燒狀況和熱效率有明顯改善。
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