排煙排熱系統 的英文怎麼說

中文拼音 [bèiyānbèitǒng]
排煙排熱系統 英文
rwa
  • : 排構詞成分。
  • : Ⅰ名詞1 (物質燃燒時產生的氣體) smoke 2 (像煙的東西) mist; vapour 3 (煙草) tobacco 4 (紙煙、...
  • : 系動詞(打結; 扣) tie; fasten; do up; button up
  • : Ⅰ名詞1 (事物間連續的關系) interconnected system 2 (衣服等的筒狀部分) any tube shaped part of ...
  • 排煙 : eject smoke; discharge smoke排煙道 smokejack; discharge flue; 排煙器 smoke ejector; 排煙裝置 fume extractor
  • 系統 : 1. (按一定關系組成的同類事物) system 2. (有條理的;有系統的) systematic
  1. Wearproof porcelain plate developed by this factory can be used as inside lining plate, coal delivery pipework, bin, bunker, separation port, wind pipe bend, exhauster, inner pipe of mill fan, air preheater, air fule and various dedust equipment for antifriction. besides, it can extend the service life of equipment

    耐磨瓷板是我廠自行研製的適用於磨煤機內襯板,輸煤管道、料倉、料斗、粗、細粉分離口、一、二次風管彎頭、引風機、粉機內殼、空氣預器、尾部道等以及各類除塵設備的防磨抗蝕、延長設備的使用壽命。
  2. Analysis of experimental data indicates that there exist several following problems during the whole operation : first, the emission is serious and the density of hc and co smoke is very high at on and off period. second, there is oil dripping from the dripping vitta as a result of the fault of ignition system and combustion structure. the last, there might be accidents of disabled ignition resulted from the improper operation at the beginning

    通過對樣機的試驗分析和研究表明,汽車空氣燃油加器在整個工作過程中,其放存在以下三個問題:一、開機和關機兩個階段的放問題嚴重,廢氣中hc和co的濃度值及度測量值都很高;二、因點火和燃燒結構的缺陷而導致開機后一段時間內有油滴從滴油管滴落;三、在點火過程中,會出現因操作不當而點火失效的現象。
  3. Wa. smoke and heat control systems - part 4 : heat exhaust systems ; test methods

    控制.第4部分:
  4. Smoke and heat control systems - part 2 : natural smoke and heat exhaust ventilators ; design, requirements and installation

    控制.第2部分:自然通風機.設
  5. Components for smoke and heat control systems - functional recommendations and calculation methods for smoke and heat exhaust ventilation systems, employing steady - state design fires - code of practice

    控制部件.利用穩態設計點火法的通風用功能推薦方法和計算方法.實施規程
  6. Components for smoke and heat control systems - functional recommendations and calculation methods for smoke and heat exhaust ventilation systems, employing time - dependent design fires - code of practice

    控制部件.利用時間相關設計點火法的通風的功能推薦方法和計算方法.實施規程
  7. For the optimization function of hrsg, the cool costs is considered as the objective function and the variables are the number of row, the number of tube per row, the horizontal distance and vertical distance between tubes of the evaporator and the economizer

    建立了以bchp的冷量成本為目標函數,以余鍋爐溫度、蒸發器和省煤器中螺旋翅片管管數、每管數、管束橫向節距和管束縱向節距為決策變量的余鍋爐優化模型。
  8. Fumes and hot air are discharged in such manner as not to be a nuisance. metal hood, air - ducts, extraction fans, grease filters water scrubbers of exhaust systems are maintained in good order

    放油空氣的方式不會造成滋擾,而的金屬罩氣槽抽氣扇油過濾器水劑滌氣均保養良好
  9. Fumes and hot air are discharged in such manner as not to be a nuisance. metal hood, air - ducts, extraction fans, grease filterswater scrubbers of exhaust systems are maintained in good order

    放油空氣的方式不會造成滋擾,而的金屬罩、氣槽、抽氣扇、油過濾器水劑滌氣均保養良好;
  10. Abstract : the causes for low efficiency of the heater in no. 2 crude unit of jpc refinery are described and analyzed including water leaking of steam soot blower, dew point corrosion caused by steam, soot deposits in convection chamber owning to poor soot blowing, high flue gas temperature, no heat recovery of flue gas, and poor performance of insulation lining, etc. by using sonic soot removing system, flue gas recovery system, spray coating of fiber and rock wool, as well as adjustment of flow scheme accordingly in the technical revamping. the dew point corrosion is completely eliminated, the insulation performance is improved, the heat loss is reduced by 1. 25 %, the flue gas temperature is reduced to about 170, and the heater efficiency is increased from 83 % to more than 90 %

    文摘:分析了金陵石油化工公司煉油廠二套常減壓裝置加爐存在的因蒸汽吹灰器漏水,蒸汽引起露點腐蝕及吹灰效果差造成對流室積灰,溫度高,量未回收利用以及爐子保溫襯里效果差等問題,提出採用聲波除灰氣回收、纖維噴塗和巖棉噴塗及相應的流程調整等改造措施.測定結果表明,本次技術改造解決了因蒸汽吹灰器漏水所造成的露點腐蝕問題,提高了保溫效果,減少散損失1 . 25 % ,溫度降至170左右,裝置的爐效率由83 %左右提高到90 %以上
  11. The causes for low efficiency of the heater in no. 2 crude unit of jpc refinery are described and analyzed including water leaking of steam soot blower, dew point corrosion caused by steam, soot deposits in convection chamber owning to poor soot blowing, high flue gas temperature, no heat recovery of flue gas, and poor performance of insulation lining, etc. by using sonic soot removing system, flue gas recovery system, spray coating of fiber and rock wool, as well as adjustment of flow scheme accordingly in the technical revamping. the dew point corrosion is completely eliminated, the insulation performance is improved, the heat loss is reduced by 1. 25 %, the flue gas temperature is reduced to about 170, and the heater efficiency is increased from 83 % to more than 90 %

    分析了金陵石油化工公司煉油廠二套常減壓裝置加爐存在的因蒸汽吹灰器漏水,蒸汽引起露點腐蝕及吹灰效果差造成對流室積灰,溫度高,量未回收利用以及爐子保溫襯里效果差等問題,提出採用聲波除灰氣回收、纖維噴塗和巖棉噴塗及相應的流程調整等改造措施.測定結果表明,本次技術改造解決了因蒸汽吹灰器漏水所造成的露點腐蝕問題,提高了保溫效果,減少散損失1 . 25 % ,溫度降至170左右,裝置的爐效率由83 %左右提高到90 %以上
  12. Air - conditioner, heat sources, cooling coils, heating coils, reheaters, smoke exhaust systems, air handling units, fan coil units, room air units, etc

    空氣調節裝置冷氣機、發線圈、冷卻線圈、加器、、風櫃、風機盤管、窗口機等
  13. Smoke and heat control installations - part 5 : powered smoke exhaust systems ; requirements, design

    控制裝置.第5部分:動力.設計要求
  14. In certain uses the limestone aqueous method desulphurization ( hereafter refers to as fgd ) in the system, after desulphurizationsmoke warm approximately 50, if does not heat up then possiblybrings the chimney to discharge the difficulty

    在某些採用石灰石濕法脫硫(以下簡稱fgd )的中,經脫硫后的溫約50 ,若不加則可能帶來放困難。
  15. Smoke and heat control systems - part 2 : specification for natural smoke and heat exhaust ventilators

    霧和氣的控制.第2部分:霧和氣口用自然通風機規范
  16. Analysis result of simulation shows : underground commercial streets and atrium can use natural filling. in the actual engineering, mechanical smoke exhaust system is used by the local fire department added. the night club uses a set of mechanical smoke exhaust system, and the quantity of supply air can ’ t be less than 50 percent of the exhaust

    模擬研究表明:地下商業街和中庭可以採用自然填充,在實際工程中當地消防部門在中庭增設機械,以加快氣的放;夜總會採用機械,補風量不應小於量的50 % 。
  17. The hight and temperature of heat smoke during the fire was obtained by using numerical simulation method, people in the bowling alley could evacuate safely was proved and the building ' s fire safety objective was satisfied

    通過數值模擬給出了發生火災時的氣層溫度和氣層高度發展過程,證實了保齡球館的水噴淋和機械能夠保證人員安全疏散,滿足消防安全要求。
  18. In this paper, performance - based fire safety design concept was adopted to analyze fire safety objective of a underground bowling alley should achieve, fire scenarios were designed and the performance of water sprinkler and mechanical smoke evacuation system was studied by using zone model

    摘要採用性能化防火設計的思想,分析了某地下保齡球館火災氣安全需求,設計了可能發生的火災場景,使用區域模擬技術研究了保齡球館水噴淋和機械的有效性。
  19. Pesents the air conditioning pattern and the design of cold and heat sources, water system, ventilation and smoke management systems, and automatic control system

    介紹了空調形式、冷源、水、通風及防、自控的設計。
  20. Smoke and heat control systems - part 2 : specification for natural smoke and heat exhaust ventilators ; german version en 12101 - 2 : 2003

    控制.第3部分:的自然放通風器規范
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