深水測深索 的英文怎麼說

中文拼音 [shēnshuǐshēnsuǒ]
深水測深索 英文
deep-sea lead line
  • : Ⅰ形容詞1 (從上到下或從外到里的距離大) deep 2 (深奧) difficult; profound 3 (深刻; 深入) thor...
  • : 名詞1 (由兩個氫原子和一個氧原子結合而成的液體) water 2 (河流) river 3 (指江、河、湖、海、洋...
  • : 動詞1. (測量) survey; fathom; measure 2. (測度; 推測) conjecture; infer
  • : Ⅰ名詞1 (大繩子; 大鏈子) a large rope 2 (姓氏) a surname Ⅱ動詞1 (搜尋; 尋找) search 2 (要; ...
  • 深水 : deepwater
  1. The method of close water test has been used for a long time, so richer experience has been achieved. however, it not only takes pains and time, but also consumes raw materials during the close water test because of miscellaneous working procedures such as bricklaying in the two ends of pipe, water - repellent layer plastering, maintaining and water offletting, brick - block backouting after the test, especially in the region short of water and some drainage pipe with prop - pipe construction. in order to satisfy the fast development of municipal construction, new detection methods should be developed

    試驗方法因其應用時間較長,目前已積累了較豐富的經驗,但在閉試驗時,管道兩端砌築磚堵、抹防層、養護、灌浸泡,以及試驗后的放、磚堵拆除等繁雜工序,不僅費工、費時,而且消耗原材料,尤其是在缺的地區以及頂管施工的無壓管道,這些矛盾更加突出;因此,為滿足迅速發展的市政建設需要,有必要探新的檢方法,閉氣試驗就是其中一種,但是閉氣試驗目前還不完善,有待于進一步入研究。
  2. During the 3d finite element calculation, try to simulate different procedure of the construction ( like sunk well in - filling, main cable erection, box girder hoist, bridge flooring and opening to traffic ). and then, reveal the regulation of deformation and displacement on the foundation and soil during different period. after got these, this thesis put great attention on the analysis of the reason which cause the horizontal displacement of the cable saddle, as well as the regulation of the pressure ' s changing in the soil located on the front side of the sunk well foundation

    在三維有限元計算中,對不同工況(沉井充填、錨體澆築、主纜架設、箱梁吊裝、橋面鋪裝以及通車運營)下的施工過程作了模擬,全面揭示了各工況下錨碇沉井基礎與地基土的變形變位規律,著重分析了影響散平位移的因素以及不同工況下沉井前地基土平向抗力變化規律,並提出了不同度地基土平向抗力與平位移間的擬合關系。
  3. Probe into mud scum and survey of navigable depth in xiashimen channels in beilun port complex of ningbo port

    寧波港北侖港區蝦峙門航道浮泥探及適航
  4. It was shown that the measured active soil pressures were smaller than the theoretical values and diminished with time, the measured pore water pressure decreased with the time and increased with the depth of soil, the combinative effects of cap girder and supporting structure were obvious which diminished the displacement of foundation pits, and the measured axial force of the anchor and interior steel beam were far less than the design force, indicating that the design safety factor of the foundation pit was too large to be economical

    基坑工程實行信息化施工並獲得了豐富的監數據,通過對數據分析結果表明:實主動土壓力小於計算主動土壓力,實主動土壓力隨時間延長變小:土體中孔隙壓力隨時間增長而減小,孔隙壓力隨度增加而呈非線性增加;基坑冠梁協同作用明顯,冠梁減小了基坑變形;錨軸力比較穩定,鋼撐軸力變化相對較大,且二者軸力仍富餘較大,該設計比較安全。
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